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Bute Sunday 5th August.

Sunday was a bit different. The tail-wagging excitement was giving way to the more usual sense of being at work and on a mission such as had always pervaded our workshop. By now we knew where our tools were and each had adopted whatever task seemed best to suit them as their own. Jersey Mike had arrived from Jersey bearing pretty much everything we could ever wish for and set up the workshop in a totally organised fashion. The tea tent was fully commissioned now too with each member of the crew having being issued a paper cup on the bottom of which we wrote our names so as not to lose their very own brew mug.

Today it was time to up the ante and start creeping up on getting K7 running at speed again on the water. First thing was to have Stew carry out a static engine run to warm all that metal and blow out the cobwebs and also to give him some engine handling experience from inside the cockpit.

But this was not your standard static because shortly before we left for Bute our engine had developed a problem that we’d thus far been unable to cure. The book says the engine should idle at 3650 rpm. In fact what it actually says is something like 3650.374 +/- 5rpm. How can you have a figure to many decimal places then slap plus or minus five on the end, we asked aerospace? It’s derived from a graph, apparently and so we were often presented with such confusing figures – oh, and don’t forget to factor in ambient air temperature and barometric pressure. We decided that somewhere near 3650 would do for our purposes, especially as the RPM indicator was mismatched to its generator on the engine and read incorrectly until we had it recalibrated by ‘Clever’ Barry Hares. Donald had a similar mismatch and never got his working properly so far as we know.

We’d therefore been happy that, from the first time it ran properly, our engine spun up to 3650-ish and sat their happily turning paraffin into noise. The way the engine is set up is that a lever down in the right hand side of the cockpit is slid forward until it locks into a detent and opens the throttle valve on the engine to thirty-four degrees, which is what’s required for start and idle. The other sixty degrees is controlled by a foot throttle. What you do next is switch on the igniters, arm the start system then hit the start button. There’s a violent whoosh somewhere behind your head followed by the whine of the compressor as it spools up. Soon the RPM indicator flickers and begins to catch up with the accelerating spool until, about three seconds in, there’s a whoomph! as the igniters do their job and the engine starts to accelerate. Now the exhaust gas temperature indicator, having arrived late at the party, suddenly leaps off its stop and climbs rapidly. You have to hold steady on the starter until the needle climbs past three hundred Celsius at which point you can release the button and the whoosh of compressed air ceases instantly. Upwards goes the EXH gauge as the temperature soars alarmingly. Four hundred, five hundred, six hundred until at last its seemingly inexorable ascent is checked by inrushing air hungrily ingested by the compressor. Seventy percent of the air that goes through the engine serves no purpose but to tear unwanted heat from the metals and throw it out the back before it damages something. Push the turbine much over seven hundred for more then a few seconds and it invisibly destroys the structure of the blades and begins to fail at that point. No ifs, no buts, you just wrecked your engine so we drummed the start procedure into our pilots.

However, the problem that now plagued us was that instead of the engine idling at 3650 as it always had, just before we left for Scotland it suddenly began settling nearer 5000 and nothing we tried would have it do otherwise. This was a problem for three reasons.

Firstly, we didn’t know why it was doing this so what if next week it decided instead of 50% it might like to idle at 75% or 100% - then we’d be in bother. Secondly, you can’t start your jet boat in neutral. Once it’s lit it starts to move and as we’d never tried lighting it on water we’d prefer if the process were as gentle as we could make it and whooshing up to 50% was unlikely to prove gentle and, finally, we’d been warned by Lew Norris years earlier about just how efficient K7 is when planing so with our engine stuck at 50% we had doubts about being able to slow down at the end of a run. Of course the pilot could just pull the lever back and the engine would shut down instantly but that would mean no return run unless we moved the whole operation to the other end of the loch to start again from there.

We initially thought we’d just set the linkage up wrong as it’s absolutely impossible to see what you’re doing down there but it is possible to adjust the linkage – just – so we ran the engine and adjusted until we had the idle we wanted. Sorted – except it wasn’t. Once shut down the engine wouldn’t re-start. Investigation revealed that our adjustment had reduced the initial opening to a mere twenty-two degrees, enough for the correct idle once the pressures came up in the system but nowhere near enough to start the engine. We were flummoxed. There’s also an adjuster on the engine called the ‘idle bypass’, which is like the idle screw on your petrol lawnmower only with extremely fine adjustment. It goes in tiny clicks because the difference between flowing lots of kerosene and none at all is minuscule – hence the issue with the incorrect SG of our fuel but no matter what we tried we couldn’t persuade it to have any effect and our friends in aerospace sadly declared it a victim of ‘magic muck’.

Magic muck is a theoretical contaminant that gets into the fine workings of hydro-mechanical fuel systems and prevents something from working properly but when dismantled there’s nothing to be seen and when reassembled it all works as it should. We had no time to go investigating magic muck so by the time we wheeled K7 out of her boatshed that Sunday morning to have Stew perform his static engine run we were stuck with our 50% idle problem and were just going to have to work around it.

After Malcolm’s safety briefing we began with the roll out.



Notice the tool benches down the left and the plethora of fire extinguishers on the right. It hadn’t taken us long to get our boat shed into shape. Also on the right in his uniform is Stew Vandal representing the army unit who installed our slipway. He made us so collectively itchy by standing in a very military way in full scratchy uniform and cap for the first couple of days that we begged him to swap it for shorts and flip flops. Stew did just that and became one of the team very quickly.



The crowds had begun to gather by the time our other Stew climbed into the cockpit. We also had a safety briefing for the crowds where we told them to protect their childrens’ ears and secure any loose items that might be swirled away into our engine. Truth be told, it only creates a mild breeze at low power settings but it was all good precautions. The spectators were brilliant and took excellent care whenever we carried out one of these tests.



Once strapped in, Stew spent some time going over the controls and doing practice drills from his checklist. This was a bit of a vertical learning curve for him but he went about it most professionally until, declaring himself satisfied, he closed the lid, gave us the signal that he was good to go and we removed the intake blanks.


It went off without a hitch. Stew followed the start procedure to the letter, the engine lit at the prescribed moment and, though yet again it raced to 50% before settling down, everything ran smoothly. We also got to see for the first time the effect of the jet efflux on the surface of the loch.


Another small glitch we took with us was a small but persistent fuel leak from part of the fuel system that operated at very high pressure. Much of the fuel system we ran on Bute was overhauled original – a seemingly impossible task undertaken for us by aerospace but which created many problems of its own one of which was choosing suitable gasket material. Back in 1959 when it was built, asbestos gaskets were the norm and what an incredible gasket material it is. Mainly because the same microscopic hooks that make it ruin your lungs also grip the sealing faces of whatever you want to seal and don’t let go but of course we can’t have those any more so the one that was leaking had been replaced with some high-performance foil-backed carbon material but unfortunately it wasn’t quite high performance enough and it leaked. You’d think all of this shouldn’t be a big deal but in many cases the thickness of the gaskets between faces of the myriad components affected the stroke of levers or the travel of pistons so it all needed careful redesign in the rebuild process. We later cured this particular leak on the test rig with a new carbon gasket and some aerograde Hylomar but in Scotland with the fuel system largely inaccessible we could only keep an eye on it so John peered in and declared it OK.



Stew’s static run lasted only a couple of minutes to conserve our limited fuel because we had a bigger plan for later in the day but it was a complete success and caused much smiling once he’d shut the valves and the engine had spooled to a standstill and the blanks went back in.



Malcolm did his debrief, all parameters were recorded in our notes then we headed for the tea tent for refreshments and a natter with the crowd who had about a million questions. Stew enjoyed a well-earned photo opportunity.



But no rest for the wicked because our rather bold plan for the afternoon was to get Bluebird onto the water, install lead-pilot Ted in the cockpit, light the engine then have him complete a slow taxi run down to where the loch narrows and then back again. That half of the loch is really shallow and we could all see it clearly from whatever vantage point so it was a good starting point for our on-water running but first we had to prepare our kit to enable us to light the engine whilst afloat.

Yet another incomplete job before our crew training was Bluebird’s on-board air start system. With the help of another sponsor from Aerospace we’d got the original working but not so we could safely use it. It was only tested to a pressure where it would spin the engine for a few seconds but nowhere near enough to start it so we’d designed in an offboard connection but now we had to get our start bottles afloat.



Stew Vandal, now out of his scratchy army uniform and looking a million times more comfy, helps Jimmy Poole (in the boat), operator of Loch Fad Fisheries and skipper of the start boat from the get-go, to try out our arrangement for stability.

We asked Jimmy, who had also been instrumental in arranging a thousand and one things on the island ahead of our arrival, to skipper our start boat as he knew these little boats better than anyone, and soon enough he became so crucial that a run would be delayed if we couldn’t find Jimmy for whatever reason. That’s basically our start rig bobbing about on a boat. It’s two, 50litre, 300Bar air bottles attached to the rapid start system from a Vulcan bomber. It all connects to Bluebird via an air hose and an electrical connection and can be fired by the pilot in the cockpit. Bute Blacksmiths allowed us to steal their 3-phase leccy to run a HP compressor to charge a second pair of bottles from which we decanted air to keep our start boat topped off.

We launched Bluebird



We knew how to do this now – crew training, you see.



One of the regular tasks was to remove the jetpipe cover once the boat was afloat. We always left it in place for the launch or a bout a hundred gallons of water was sluiced straight up the spout. John wades ashore with it.



Then, with us all back on the beach, Sir Malcolm presided over one of his pre-run briefings. We had lots of things to discuss this time as what we were about to do was very daunting and we’d never done anything like it before. It was quite scary to think that the big, inanimate lump from our workshop was soon to become the jet-powered boat she’d been designed to be. Of course this had always been the plan but it had also always been pie in the sky for so many years. Imagine how it felt to be stood at the side of the loch about to really do it for the first time!



This was it then, the big one, but even after all our preparations we still had things to puzzle out, like how to get Ted safely into the cockpit from a bobbing safety boat. An ongoing difficulty with Bluebird is the compromise between her unbelievable strength underneath where all the hard work is done and how lightly her upperworks are constructed to minimise weight. One foot planted in the wrong place could push a dent in a panel that would take weeks to repair. That’s why the sponson tops had ‘do not stand here’ written across them in big letters – presumably Donald got well fed up with people clumsily denting his boat – so we had to get Ted aboard without him squishing anything delicate, without him slipping and hurting himself or anyone else and without him leaving any sand or gravel on deck from where it could be sucked into the engine.

We spent a good while out there messing about making sure we had a reliable way of getting Ted into the cockpit. Of course, it would have been easier to install him before we launched but we still needed practice with our launches so we left the pilot out of the mix just in case. Notice how most of us are just standing around on the lakebed. Despite being way out in the middle the water is only chest deep.



Next came the problem of starting the engine whilst afloat and we were also learning fast that that huge fin up there, far from doing anything useful, was just a pest. The tiniest breeze would swing Bluebird this way and that making Jimmy’s job of holding station with the starting boat an awful task. Once securely alongside, John then had to connect the air and the electrical connector then remove it again once the engine was running and before both boats began to move because they were tied together. The biggest problem here was that John and Jimmy had no direct communication with Ted so a control boat was later added to take care of the comm’s but today, seeing as the safety boat was remaining in the immediate locale, we elected to do the controlling from there so as to remove one of the boats from the equation. This was my job while Sir Malcolm took care of overall operations from the slipway.



Jimmy took the start boat alongside so John could remove the intake blanks then they slipped down to the starboard side and made the connections, holding both boats on station while everything else was prepared.



Malcolm could be heard on the radio asking the safety boat to report on the wind and surface conditions. Down in the narrows where the breeze was funnelled both could get confused in a way that wasn’t evident from where we were watching but we weren’t going that far today so it wasn’t a problem. Jordan was soon back on the radio and his observations logged for future. Malcolm then handed over to us on the safety boat and I signalled John to ensure all was good over there – it was.

Next I signalled Ted to say the start crew was ready – he’d heard the radio chatter and knew the course was his but we didn’t want to trust radio comms between Ted and the start boat because of all the noise they promised to find themselves amongst yet the scene was eerily quiet. The anticipation had left the crowds with no words and the crackle of the radios sounded deafening and almost intrusive amongst it.

Ted sat quietly in his office completing his drills for a moment and doubtless contemplating the immensity of the moment then he slid the canopy shut, tightened his belts, lowered his visor and held up three fingers to ask for the countdown to startup.

“Three – two…” I boomed over the hushed loch, “One…” a half a beat pause then, whoosh!

Bluebird’s engine spun up and lit just as expected and the efflux, now within inches of the water, began to tear strips off the surface and blast it into an angry maelstrom of spray. She began to move too, taking the start boat with her. Then Ted’s left hand shot upwards – the signal that he was off the starter and the light was a success. I saw John staring intently, waiting for me to give the signal to make the disconnects. I flashed him the diver’s OK signal – one we were very used to using – and in seconds Bluebird was free. John flashed OK back to me and me to Ted. He was on his own now.

There then followed one of the most hilarious things we had ever seen that, regrettably, seems not to have been captured by any camera. We were on the same side as the start boat so saw it all clearly but it was lost to everyone else.

As Bluebird began to move, Jimmy allowed the small boat to simply fall back and away from the advancing gas turbine but all that happened was that they were slurped into the low pressure area at the side of the efflux and comprehensively hosed down with warm water. The last image of John before he disappeared completely was of him apparently trying to decide whether or not to leap overboard while Jimmy first stood there having his front soaked only to decide he wasn’t keen on that so he turned around to have his back done too.



It would have been much funnier had they been blown overboard but we decided we needed to think again about on-water starting. Crew training, once again.

But by now Bluebird was off and what a sight as she powered away from us! From our boat a plume of spray soon blotted out any sight of the boat but the roar of the jet still thundered around the valley whilst the direct sound was dampened almost out of existence by the spray. And then Ted turned slowly and began heading back and we got a proper look.

Then we heard the engine spool up and Bluebird climbed higher and higher out of the water. This was amazing! So many times we’d read of how marginal she was for getting up on the plane, how Donald had affixed sand bags and lead ingots – that we’d dutifully put back – and how this whole planing thing was a delicate and almost unobtainable nirvana yet here we were on a low power setting just about doing exactly that.



But Ted had very strict orders. Not to go very far and most definitely not to go very fast. If Paraffin Pete could come up with the good stuff tomorrow we might look at going a little quicker but today had been another big success so we’d take that to the bank. We brought him ashore.



It was an awesome moment. You couldn’t imagine how incredibly special it was to have worked so hard for so many years for moments like these and then been able to just enjoy them because it all went to plan.



The media were loving it too and we spent a good while in front of the cameras after that one.



Good old Kersh was in the thick of it as ever.





We knew that we were getting good results because of the incredible amount of preparation that had gone in beforehand and not just because of the engineering, the planning and teamwork was first class too and we were almost making this look easy but we had to stay focussed. Next job was to recover Bluebird and carry out a thorough inspection.



Dave brought the AA van down to the water where Jersey Mike had essentially become team leader of the launch and recovery crew so it didn’t take long to get the boat back up on the dolly and onto the slipway but once again we’d shipped an awful lot of water and once again it hosed out when we hit the pumps.



We had expected to ship some this time because there was an awful lot of it flying around but surely not this much. At least by now the hull had been washed out by our earlier exploits and we could just pump it out. But where was it getting in? This remained a worrying mystery but even worse was that one of our sponsons had filled up too and that just wasn’t possible.

It’s well recorded that Bluebird’s original sponsons very quickly filled with water when she was first launched on Ullswater so upon Ken Norris’s instructions the crew opened each compartment with a small hole in the top and filled them with expanding foam. But this was concurrent with the ballast tanks built at her rear refusing to remain watertight too and these were finally cut away so those involved likely just assumed the sponsons leaked in the same way. Indeed, Ken instructed the builders on his drawings to ‘fill any large gaps with Loy filler’, car bodge in other words. Yet he didn’t draw any large gaps so what was he expecting?

Then, if you study archive shots of Bluebird you will see over the years that a set of drain bungs was added to the rear face of the float wedges and then a second set higher up presumably to allow air to enter to speed the draining process. We included them for historical accuracy but our sponsons weren’t going to leak a drop.



There are three longitudinal channels in there so three sets of bungs but we took immense care to make sure there were no gaps anywhere and every millimetre was sealed and sealed again with the dreaded choccie sauce yet, soon as we returned from our low speed test and removed the bungs…



Mike tirelessly looked after all the ongoing maintenance beginning early in the day before anyone else, except Jersey Mike who actually lived on site in his van, had arrived so the bungs were soon whipped out and to our consternation what followed was a seemingly endless spurt of water – this just wasn’t possible.

We took the top off the sponson and to our horror it was half full.



We had no answer to this. All we could do was keep an eye on it. Unlike the main hull we could thoroughly inspect every millimetre of the sponson whilst out of the water and it most definitely did not have any holes in it. We knew there was a small amount of ingress past the top covers because they were a compromise. We’d had to be a little minimal when sealing them down in case they had to be removed and also they’d definitely have to come off after we returned to base so we could have a good old strip inspection and spanner check but that couldn’t account for the ridiculous amount of water down in the sponson core. We’d not bottom this mystery for many weeks until we were safely back in Bluebird’s workshop with the sponsons dismantled and what we discovered would appear to be a gotcha that also caught out Donald and Ken back in the day.

All we could do was dry it out and button it up again. The other side seemed dry so we left that one alone.



The sponson lid went down with choccie then the screws went back in. The crew worked extra late to check every last nut bolt and rivet and it was getting dark by the time we had everything back together.



We also took off the engine cover for a thorough inspection under there. The water ingress was massive. Partly past the ill-fitting cover itself, which had allowed water to gush over the igniter wiring and that was to catch us out the following day, and partly because the problem of jetpipe cooling was one we inherited from the 66/67 crew that they never bottomed and we will have to sort out before we next run.

When K7 arrived at Coniston in 66 there was a square hole in the left-hand side of the tail cover beneath the fin but before long that was blanked off (with a piece of hardboard) and another smaller one appeared on the other side.

On the Orph there’s an inner and outer jetpipe. The inner is full of hot gas and made of nimonic stainless, the outer is aluminium and a bit longer and fatter with a stainless end where the hot gas finally meets it. The idea is that the fast-moving efflux creates a vacuum in the gap between the two into which air is drawn to cool the inner pipe. It draws the air through a pair of ports on either side of the outer jetpipe right where those holes appeared on the sides of the tail cover. One port is attached to ram-air duct on the aircraft – useless therefore when the plane isn’t moving – so the other has an inward flapping, spring-loaded door that gets sucked open when the engine is running but the plane isn’t moving. Once in flight the ram-air side provides more air therefore shutting the spring-loaded door on the other side and providing good cooling for your jetpipe.

Now then, fail to plumb those ports adequately to the outside of your jet hydroplane and what you get is just a massive vacuum under the top covers that sucks any airborne water, and we made lots of that, straight in through any opening no matter how small such that when you take the covers off it looks like there’s been a tropical rainstorm in there from one end to the other. We really need to mend that.

Notice also on the above pic a small, grey cylinder on the side of the engine behind the panel with the electrical plug in it. That was yet another mechanical issue we ran out of time to bottom and the cylinder you see is a spare, piggy-backed into the system because of another gotcha but more of that next time. The two black electrical plugs in the panel are for charging the batteries. The batteries run the pumps, igniters and provide power for the fire suppression system but there’s no generator on board so they have to be maintained in a charged condition while on shore.

Finally, with our maintenance visit complete and the boat buttoned up we pulled her back under cover for the night.



The only remaining job was to put the ends back in the boatshed, tidy our tools then retire for a shower, some food and a few beers.

By now we had made the Black Bull on the sea front at Rothesay a sort of unofficial HQ, not because it was better than anywhere else but simply because most of the crew were billeted above it. The town has several good pubs and restaurants and the island offers even more but it just became too easy to go downstairs so that’s where we went. Assuming that Paraffin Pete got us the proper juice next day we’d fuel up Bluebird and push on towards some longer runs and higher speeds.

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